吴帅,王长鹏,苏艳,陈喜栋,张凯,赵丽旸.18CrNi4WA 钢渗碳针阀体开裂失效分析[J].装备环境工程,2018,15(7):75-79. WU Shuai,WANG Chang-peng,SU Yan,CHEN Xi-dong,ZHANG Kai,ZHAO Li-yang.Cracking Failure of Carburized Injector Valve of 18CrNi4WA Steel[J].Equipment Environmental Engineering,2018,15(7):75-79.
18CrNi4WA 钢渗碳针阀体开裂失效分析
Cracking Failure of Carburized Injector Valve of 18CrNi4WA Steel
投稿时间:2018-04-27  修订日期:2018-07-25
DOI:10.7643/ issn.1672-9242.2018.07.016
中文关键词:  针阀体  18CrNi4WA 钢  失效分析
英文关键词:injector valve  18CrNi4WA steel  failure analysis
基金项目:
作者单位
吴帅 西南技术工程研究所,重庆 400039 
王长鹏 西南技术工程研究所,重庆 400039 
苏艳 西南技术工程研究所,重庆 400039 
陈喜栋 西南技术工程研究所,重庆 400039 
张凯 西南技术工程研究所,重庆 400039 
赵丽旸 中国船舶工业综合技术经济研究院,北京 100081 
AuthorInstitution
WU Shuai Southwest Research Institute of Technology and Engineering, Chongqing 400039, China 
WANG Chang-peng Southwest Research Institute of Technology and Engineering, Chongqing 400039, China 
SU Yan Southwest Research Institute of Technology and Engineering, Chongqing 400039, China 
CHEN Xi-dong Southwest Research Institute of Technology and Engineering, Chongqing 400039, China 
ZHANG Kai Southwest Research Institute of Technology and Engineering, Chongqing 400039, China 
ZHAO Li-yang China institute of marine technology and economy, Beijing 100081, China 
摘要点击次数:
全文下载次数:
中文摘要:
      目的 研究18CrNi4WA 钢渗碳针阀体开裂失效原因。方法 通过化学成分分析、断口扫描分析、金相组织分析、能谱分析等测试手段,对 18CrNi4WA 钢渗碳针阀体的断裂模式及失效原因进行分析。结果 针阀体失效件原始材料符合针阀体制造要求,但渗碳淬火温度过高,未得到最优的渗碳层组织,燃油中存在的硫元素导致喷油孔位置产生严重腐蚀,燃油局部压力的变化导致针阀体表面产生空蚀损伤,裂纹起始于喷油孔圆周面,自裂纹源向外发散呈月牙状,为典型疲劳断裂特征。结论 腐蚀与空蚀损伤的协同作用加快裂纹的萌生,使针阀体在热疲劳及机械振动等交变载荷的作用下产生疲劳开裂,使用寿命大为降低。
英文摘要:
      Objective To investigate cracking failure reasons of the carburized injector valve made of 18CrNi4WA steel. Methods The fracture modes and failure reasons of the injector valve were analyzed by means of chemical composition analysis, SEM analysis, metallographic examination and energy spectrum analysis. Results The original material of the needle valve was in conformity with the manufacturing requirement. But due to the high carburizing quenching temperature, the best carburized layer structure was not obtained. The sulfur element in fuel caused serious corrosion of injection holes. Changes of the local pressure in the fuel oil caused cavitation damage on the surface of the needle valve body. The crack began at the circumferential surface of the injection hole and radiated from the crack source to the crescent shape. It was called as typical fatigue fracture. Conclusion Synergistic effects of the corrosion and cavitation damage promote crack initiation and produces fatigue cracking under the action of the thermal-mechanics alternate fatigue load. The service life of the injector valve was greatly reduced.
查看全文  查看/发表评论  下载PDF阅读器
关闭

关于我们 | 联系我们 | 投诉建议 | 隐私保护 | 用户协议

您是第11976655位访问者    渝ICP备15012534号-5

版权所有:《装备环境工程》编辑部 2014 All Rights Reserved

邮编:400039     电话:023-68792835    Email: zbhjgc@163.com

视频号 公众号